Thursday, January 4, 2024

Saga Continues For DEP Trying To Get A Conventional Operator To Plug Warren County Well Venting Gas Since At Least 2018

The continuing saga of trying to get
Tatonka Oil Co. LLC-- an Ohio-based company-- to plug the Nancy 13 conventional gas well in Deerfield Township, Warren County that was found to be leaking brine and gas since at least December 20, 2018 -- continues.  [Read prior history here.]

On February 8, 2019, a DEP inspection report said Commonwealth Court had issued an order to Tatonka Oil Co. LLC to plug a number of wells it operated, including the Nancy 13 well.  [DEP inspection report]

DEP inspections documented repeated violations at Nancy 13, but finally on May 17, 2023 an inspection report noted Tatonka said the plugging of Nancy 13 would start in April or May.  [DEP inspection report]

And now an update….

On June 7, 2023, a DEP inspection report said Tatonka Oil retained Oil Valley Well Service to “replug” the Nancy 13 well, but no start date was established. [DEP inspection report

On November 8, 2023, a DEP onsite inspection occurred to review well records, bond log and certificate of plugging submitted to DEP on May 4, 2021. 

The report notes gas was still bubbling up through the well. 

“Operator is planning to have contractors clean out the well-bore and drill out cement plugs to determine where the gas is coming from. Once it is confirmed where the gas is coming from contractors will start plugging the well. Operator and contractors will notify the department throughout the process.” [DEP inspection report]

On December 12, 2023, the Department received a notice from Tatonka Oil that plugging contractors were going to start moving equipment onsite December 11, 2023.  Onsite inspection December 12, 2023 found the contractors have not moved onto the location. [DEP inspection report

On December 21, 2023, an onsite inspection showed plugging contractors have started making preparations-- dug a waste pit and lined it, but will not start drilling until after the Christmas holiday. [DEP inspection report]

On January 2, 2024, the initial report to DEP on plugging had contractors drilling out the well to a depth of 500 feet.  [DEP inspection report

However, a followup phone conversation with the contractor found a depth of 1,020 feet was reached, but circulation of water to clean out the well bore has been unsuccessful and the drill pipe may become stuck if drilling continues. 

“If circulation cannot be obtained, the well may be plugged from an attainable bottom of 1,020 feet with a solid column of cement to the surface casing seat.” [DEP inspection report

On January 3, 2024, the contractor told DEP they could not clean out the well below 1,020 feet so 32 barrels [1,344 gallons] of cement were put in place from 475 to 1,020 foot depth in the well.  The drill pipe is being pulled from the well and drill cuttings and wastewater are contained in a lined pit on the site. [DEP inspection report]

DEP eFACTS records show Tatonka Oil Co. LLC operates 149 conventional oil and gas wells in Pennsylvania.

Report Violations

To report oil and gas violations or any environmental emergency or complaint, visit DEP’s Environmental Complaint webpage.

Check These Resources

Visit DEP’s Compliance Reporting Database webpage to search their compliance records by date and operator and the Inspection Reports Viewer.

Sign up for DEP’s eNOTICE service which sends you information on oil and gas and other permits submitted to DEP for review in your community.

(Photo: Nancy 13 from November 8, 2023 DEP inspection report.)

PA Oil & Gas Industry Public Notice Dashboards:

-- PA Oil & Gas Weekly Compliance Dashboard - Dec. 30 to Jan. 3 - Saga Of Plugging Nancy 13; Conventional Well Emission Offsets; Venting Since June; Still No Well Integrity Reports  [PaEN]

-- PA Oil & Gas Industry Compliance So Far In 2023 - It Isn’t Pretty   [PaEN]

-- PA Oil & Gas Industrial Facilities: Permit Notices/Opportunities To Comment - January 6  [PaEN]

-- DEP Disapproves Land Recycling Risk Assessment For Dozens Of Chemicals At American Refining Group Refinery In Bradford, McKean County  [PaEN] 

-- DEP Reviewing Act 2 Cleanup Reports For Trainer Refinery, Delaware County; Philadelphia Energy Solutions Refinery  [PaEN] 

-- DEP Posted 49 Pages Of Permit-Related Notices In January 6 PA Bulletin  [PaEN]

Related Articles This Week:

-- DEP: Shale Gas Operator Found Responsible For Water Supply Contamination After Investigation Documents Chemical Contamination Spread Across 3 Townships In Greene County  [PaEN] 

-- DEP Accepting Project Applications For $5 Million Shell Petrochemical Plant Beaver County Environmental Mitigation Community Fund  [PaEN]

-- Zefiro Methane Corp To Begin Monitoring Abandoned Conventional Wells For Plugging To Create Emission Offsets [PaEN]

-- Saga Continues For DEP Trying To Get A Conventional Operator To Plug Warren County Well Venting Gas Since At Least 2018  [PaEN]

-- Penn State Extension To Host Jan. 18 Webinar On Unlocking The Power Of Hydrogen  [PaEN]

-- PJM Urges United Action To Sustain Grid Reliability Through The Energy Transition, Avoid Unreliability Issues Of Natural Gas, Other Generators  [PaEN] 

NewsClips:

-- Bob Donnan Blog: Fracked Up Greene County Water - Shale Gas Operator Found Responsible For Water Supply Contamination

-- PennLive Guest Essay: Gov. Shapiro Has Done An About-Face On Fracking By Aligning Himself With CNX After Charging Them With Environmental Crimes - By Karen Elias, Climate Reality Project, Better Path Coalition

-- Bob Donnan Blog: Frack History - The Massive Dunkard Creek Fish Kill  

-- Bob Donnan Blog: Dunkard Creek Fishkill In Greene County Caused By Consol Mine Discharge [Video] 

-- TribLive Guest Essay: Celebrating EPA’s New Safeguards To Reduce Methane Emissions From Oil and Gas Facilities - By Vanessa Lynch, Moms Clean Air Force 

-- TribLive: Lack Of Snow, Rainfall Factors In Declining Beaver Run Reservoir Levels In Westmoreland; Natural Gas Drillers Prohibited From Withdrawing Water 

-- TribLive: 4 Mile Long Diesel Fuel Spill Shuts Down Route 66 From Apollo To Vandergrift In Westmoreland County

-- Post-Gazette: Casey Says Proposed DOE Rule Could Hurt Efforts To Develop Hydrogen Industry In PA

-- The Allegheny Front: Proposed Federal Hydrogen Tax Credit Rules Could Be Worth Billions For Projects, Including Those In PA  

-- Pittsburgh Business Times: Diversified Energy Sells Unknown Number Of Conventional Oil & Gas Wells In PA, WV, OH

-- WSJ: Southwestern Energy, Chesapeake Energy Natural Gas Producers Near $17 Billion Merger

-- Post-Gazette - Anya Litvak: Peoples Natural Gas Asks Regulators For Rate Increases For All Customers 

-- Reuters: US DOE Approves $189 Million Loan For Real-time Methane Oil And Gas Facility Monitoring Network In Permian Basin

-- Reuters: US Natural Gas Producers Seek To Balance Production Cuts, Demand Rebound

-- Bloomberg: A No-Show Winter Is Upending The US Natural Gas Market Pulling Down Prices By About 35%

-- WSJ: US Shale Drillers Keeping World Awash In Oil, Natural Gas As Conflicts Abound

-- E&E News Energy Wire: 4 Oil And Gas Issues To Watch In 2024

[Posted: January 4, 2024]  PA Environment Digest

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